Consumer Complaint Detail

FREIGHTLINER / XC MOTORHOME CHASSIS / 2004

Recalls
0 Injured
Investigations
0 Death
Complaints
No Fire
Components - Details
NHTSA Complaint Number: 005025697 Incident Date: May, 05 2005
Consumer's City: APPLETON Consumer's State: WI
Vehicle Transmission Type: AUTO Manufacturers Name: FREIGHTLINER LLC
Model Name: XC MOTORHOME CHASSIS Model Year: 2004
Vehicle Involved in a Crash: No Component's Description: Steering
Vehicle Involved in a Fire: No Persons Injured: 0
Vehicle's VIN#: 4UZAAHAK44C Date added to File: May, 23 2021
Date Complaint Received: Jun, 22 2005 Complaint Type: IVOQ
Incident Reported To Police: No Purchase Date: Feb, 25 2004
Was Original Owner: No Anti-lock Brakes: No
Number of Cylinders: 6 Date of Manufacturer: -
Was Vehicle Towed: - Description of the Complaints: Loud banging noise between driver and passenger seats. sounds like wheel may be coming off axle. steering wonders and has too much free play in steering wheel. believed to be a safety issue. took to newmar to have it road tested. newmar sent to freightliner service dealer in south bend. 5/06/05 south bend freightliner service dealer stated sway bar hitting rf spring and front lower shock bolts loose. adjusted ride height 1/4 inch and inflated back tires for 80 to 110 psi. adjusted front brakes. this did not fix the problem. service dept would not state if rv was safe to drive. 5/12/05 took rv to my service company to be checked for same complaint. because freightliner service person would not or could not give warranty authorization, they shimmed stabilizer bushings with two washers on top and two on bottom of bushing which should provide a more safe ride to the freightliner factory in south carolina. master fleet stated bad steering wandering problem, possible play in steering box. tightened loose bolts. pounding noise still in front end. 6/09/05 appointment with freightliner set for two days. play in steering checked drag links, tie rods and shocks - mechanic stated ok. front end banging noise - mechanic stated tightened right front spring bolt -bushings ok. requested unit to be aligned. mechanic stated alignment ok. this took 21/2 hours. of a two day schedule. went back in the next day. bolts which were tighten were on the axle support which were to be torqed at 600 ft lbs. rv was put on lazer alignment -rv was out of alignment. left side axle support nut over torqued. both nuts were replaced. bolts were not replaced. still believe there is a safety issue. when the rv has only been traveling a few miles the steering is better than when it has warmed up. if two curves are back to back the steering wheel must be over compensated for the next curve. wind and large trucks requires for over compensation of the steering wheel.